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CN1257118C - Integrated treatment process for discharge of gas well production wastewater up to standard - Google Patents

Integrated treatment process for discharge of gas well production wastewater up to standard Download PDF

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CN1257118C
CN1257118C CNB200410019246XA CN200410019246A CN1257118C CN 1257118 C CN1257118 C CN 1257118C CN B200410019246X A CNB200410019246X A CN B200410019246XA CN 200410019246 A CN200410019246 A CN 200410019246A CN 1257118 C CN1257118 C CN 1257118C
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filler
tank
wastewater
water
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CN1579968A (en
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季民
孙忠
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Tianjin University
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    • YGENERAL TAGGING OF NEW TECHNOLOGICAL DEVELOPMENTS; GENERAL TAGGING OF CROSS-SECTIONAL TECHNOLOGIES SPANNING OVER SEVERAL SECTIONS OF THE IPC; TECHNICAL SUBJECTS COVERED BY FORMER USPC CROSS-REFERENCE ART COLLECTIONS [XRACs] AND DIGESTS
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Abstract

The present invention relates to an integrated processing technology for wastewater extracted from a gas well to achieve the effluent standard, and belongs to a processing technology for wastewater of oil-gas fields. The integrated processing technology comprises the following processes: a technology unit of the compounding and emulsion breaking reaction, a technology unit of the air flotation and separation by a Nikuni pump, a technology unit of a coarse filtering pool, a technology unit of a biofilm reactor with a hydrolysis and acidification reluctance floating bed, a technology unit of a biofilm reactor with an aerobic moving bed, and a technology unit of an aeration biologic filtering pool. The present invention has the advantage that the wastewater pollutant removing efficiency is high; the running expense is low; the management is simple; the present invention is suitable for the manufacture of integration equipment, and the integration equipment is arranged on the fields of medium and small natural gas exploitation stations. The equipment has good removing effect on main pollutants of water organic matters (COD, BOD), petroleum oil, ammonia nitrogen, sulphides, suspended substances (SS), and the like exploited from gas stations.

Description

气井采出废水达标排放的集成化处理工艺Integrated treatment process for discharge of gas well production wastewater up to standard

技术领域technical field

本发明涉及一种气井采出废水达标排放的集成化处理工艺,属于油气田废水处理技术The invention relates to an integrated treatment process for the up-to-standard discharge of gas well production wastewater, which belongs to the oil and gas field wastewater treatment technology

背景技术Background technique

目前气井采出水的处理以物化方法为主,主要注重难降解有机物的去除,一般规模较小,且处理费用较高,处理的污染物也比较单一,多数尚处于研究阶段,还没有真正用于生产的工程。目前国内在处理气井采出水的试验研究中还没有采用生物处理技术的工艺。At present, the treatment of gas well produced water is mainly based on physical and chemical methods, mainly focusing on the removal of refractory organic matter. Generally, the scale is small, the treatment cost is high, and the pollutants treated are relatively simple. Most of them are still in the research stage and have not been used in real production engineering. At present, no biological treatment technology has been adopted in the domestic experimental research on the treatment of gas well produced water.

采用沉降-吹脱-臭氧化技术处理气井水,该水中主要污染物为有机物、油类、硫化物及悬浮物等,在吹脱气量Q=1.0L/min、吹脱时间25min、臭氧浓度为14.5mg/L的情况下,取得了较好的效果。Sedimentation-blowing-ozonation technology is used to treat gas well water. The main pollutants in the water are organic matter, oil, sulfide and suspended solids. In the case of 14.5mg/L, better results have been achieved.

采用内电解法脱除气田水中的COD,内电解法是利用废水中有些组分易被氧化、有些组分易被还原,当这些不同属性组分相遇,且有导电介质时,化学反应便会自发进行的一种废水处理方法。进水COD值为250~600mg/L,控制pH为4.0,HRT1.0h的情况下,其出水COD<150mg/L。该方法存在反应速度较慢且受pH值影响大的影响,而且不适合高浓度废水的处理。The internal electrolysis method is used to remove COD in the gas field water. The internal electrolysis method uses the fact that some components in the wastewater are easily oxidized and some components are easily reduced. When these components with different properties meet and there is a conductive medium, the chemical reaction will occur. A method of wastewater treatment that is carried out spontaneously. The influent COD value is 250-600mg/L, the pH is controlled at 4.0, and the effluent COD is less than 150mg/L under the condition of HRT1.0h. This method has a slow reaction rate and is greatly affected by the pH value, and is not suitable for the treatment of high-concentration wastewater.

采用混凝沉降-微电解-氧化-吸附法处理气井水采出水。整个实验在实验室进行,可分为4步,第一步通过正交实验确定混凝沉降最佳处理配方:聚合硫酸铁(PFS)400mg/L,pH值为7;第二步在pH为1的条件下Fe/C微电解25min;第三步漂白粉氧化,投量为8g/L,氧化时间20h;第四步活性炭吸附,活性炭投加量为8mg/L,平衡时间40min,可使原水COD值从1,567mg/L降至150mg/L,其他各项污染指标达到国家综合污水排放2级标准,但该方法操作复杂,处理成本偏高。Coagulation sedimentation-micro-electrolysis-oxidation-adsorption method is used to treat produced water from gas wells. The whole experiment is carried out in the laboratory, which can be divided into 4 steps. The first step is to determine the optimal treatment formula of coagulation settlement through orthogonal experiments: polyferric sulfate (PFS) 400mg/L, pH value is 7; the second step is at pH Under the condition of 1, Fe/C micro-electrolysis for 25 minutes; the third step of bleaching powder oxidation, the dosage is 8g/L, and the oxidation time is 20h; the fourth step is activated carbon adsorption, the dosage of activated carbon is 8mg/L, and the equilibrium time is 40min, which can make the raw water The COD value dropped from 1,567mg/L to 150mg/L, and other pollution indicators reached the national comprehensive sewage discharge level 2 standard, but the method is complicated to operate and the treatment cost is high.

采用双氧水氧化和活性炭吸附联合作用的方法处理气井采出水,在小试规模下H2O2加量为0.8mL/100mL废水,活性炭投加量为4g/L,COD的总去除率可达81.8%。The combined method of hydrogen peroxide oxidation and activated carbon adsorption is used to treat the produced water of gas wells. On a small scale, the dosage of H 2 O 2 is 0.8mL/100mL of wastewater, the dosage of activated carbon is 4g/L, and the total removal rate of COD can reach 81.8 %.

国外针对气井采出水的专项性研究较少,一般针对的是整个油(气)田产出水。如连续流活性污泥处理系统处理美国西南油田产出水,在污泥停留时间(SRT)20d,混合液悬浮固体浓度(MLSS)730mg/L的条件下,对废水中的石油碳氢化合物(TPH)去除率达到98-99%。采用小试规模的反渗透-湿地处理工艺处理采油废水,整个工艺对电导率和总溶解性固体(TDS)的去除率分别达到94%和95%。采用粗粒化+膜生物反应器组合工艺处理油田产出水,通过粗粒化去除废水中的大颗粒物质,通过膜生物反应器去除其中的溶解性污染物,在水力停留时间(HRT)12h的条件下,对COD、TOC、苯酚和氨氮的去除率分别达到65%、80%、65%和40%,最终工艺出水COD和TOC为230和55mg/L。In foreign countries, there are few specific studies on the produced water of gas wells, and generally focus on the produced water of the entire oil (gas) field. For example, the continuous flow activated sludge treatment system treats the produced water of Southwest Oilfield in the United States. Under the conditions of sludge retention time (SRT) 20d and mixed liquid suspended solids concentration (MLSS) 730mg/L, the petroleum hydrocarbons in the wastewater ( TPH) removal rate reaches 98-99%. A small-scale reverse osmosis-wetland treatment process is used to treat oil production wastewater, and the removal rates of conductivity and total dissolved solids (TDS) of the whole process reach 94% and 95% respectively. Coarse granulation + membrane bioreactor combination process is used to treat oilfield produced water. Large particles in wastewater are removed through coarse granulation, and dissolved pollutants are removed through membrane bioreactor. The hydraulic retention time (HRT) is 12h. Under certain conditions, the removal rates of COD, TOC, phenol and ammonia nitrogen reached 65%, 80%, 65% and 40%, respectively, and the final process effluent COD and TOC were 230 and 55mg/L.

发明内容Contents of the invention

本发明的目的在于提供一种气井采出废水达标排放的集成化处理工艺,该工艺去除气井采出废水中污染物效率高,运行费用低。The purpose of the present invention is to provide an integrated treatment process for the standard discharge of gas well production wastewater, which has high efficiency in removing pollutants in gas well production wastewater and low operating costs.

本发明是通过下述技术方案加以实现的,对于气井开采过程中排出的含有石油碳氢化合物,硫化物,氨氮及悬浮物的废水,达标排放的集成化处理工艺,其特征在于包括以下过程:The present invention is realized through the following technical scheme, for the waste water containing petroleum hydrocarbons, sulfides, ammonia nitrogen and suspended solids discharged in the gas well exploitation process, the integrated treatment process of up-to-standard discharge is characterized in that it includes the following process:

1、混凝破乳反应工艺单元:在搅拌速度80-100转/min下,向采出废水加入混凝破乳剂聚合硫酸铁或聚合氯化铝,混凝破乳剂配比质量百分比浓度为5~10%,在气井采出废水含CODcr为2000~50000mg/L的情况下,混凝破乳剂的投加量为50~500mg/L,反应时间控制为3~10min;1. Coagulation and demulsification reaction process unit: at a stirring speed of 80-100 rpm, add coagulation and demulsification agent polyferric sulfate or polyaluminum chloride to the produced wastewater, and the coagulation and demulsification agent has a mass percentage concentration of 5 ~10%, when the COD cr content in gas well production wastewater is 2000~50000mg/L, the dosage of coagulation demulsifier is 50~500mg/L, and the reaction time is controlled at 3~10min;

2、尼克尼气泵气浮分离工艺单元:采用竖流气浮分离工艺,泵的水流量控制为0.1~0.2m3/h,吸气量占进水量的5%~10%,气浮池接触区停留3~5min,分离区停留时间30~60min;溢流排除浮渣,清水由池底穿孔管引出;2. Nickel air pump air flotation separation process unit: vertical flow air flotation separation process is adopted, the water flow of the pump is controlled at 0.1-0.2m 3 /h, the suction volume accounts for 5%-10% of the influent water, and the contact area of the air flotation tank stays 3 to 5 minutes, the residence time in the separation zone is 30 to 60 minutes; the overflow removes scum, and the clear water is drawn out from the perforated pipe at the bottom of the pool;

3、粗滤池工艺单元:池内装滤料的粒径级配为5~10mm,2~5mm的颗粒型滤料,滤料层高度为0.7~1.0m,垫层为砾石,高度0.2~0.3m,滤池操作滤速为6~8m/h;3. Coarse filter tank process unit: the filter material in the pool has a particle size gradation of 5-10mm, 2-5mm granular filter material, the height of the filter material layer is 0.7-1.0m, and the cushion layer is gravel, with a height of 0.2-0.3 m, the operating filtration rate of the filter is 6-8m/h;

4、水解酸化厌氧浮动床生物膜反应器工艺单元:反应器投加轻质生物膜颗粒填料,以填料的堆积体积计,填料投加量占池总体积之比为50%~70%,当进入生物膜反应器废水的CODcr为400~2000mg/L时,操作有机负荷为1~5kgCODcr/(m3池容·d),水力停留时间5~8h;4. Process unit of hydrolytic acidification anaerobic floating bed biofilm reactor: light biofilm particle filler is added to the reactor. Based on the bulk volume of the filler, the ratio of the amount of filler to the total volume of the tank is 50% to 70%. When the COD cr of wastewater entering the biofilm reactor is 400-2000mg/L, the operating organic load is 1-5kgCOD cr /(m 3 tank capacity d), and the hydraulic retention time is 5-8h;

5、好氧移动床生物膜反应器工艺单元:移动床生物膜反应器中也投加轻质生物膜颗粒填料,并在该反应器底部设置曝气装置,以填料的堆积体积计,填料投加量占池总体积之比为50%~70%,操作有机负荷为0.5~2kgCODcr/(m3池容·d),水力停留时间5~8h,曝气量与进水量之比为3~10∶1;5. Process unit of aerobic moving bed biofilm reactor: light biofilm particle filler is also added to the moving bed biofilm reactor, and an aeration device is installed at the bottom of the reactor. The ratio of the amount added to the total volume of the tank is 50% to 70%, the operating organic load is 0.5 to 2kgCOD cr / (m 3 tank capacity d), the hydraulic retention time is 5 to 8h, and the ratio of aeration to water inflow is 3 ~10:1;

6、曝气生物滤池工艺单元:曝气生物滤池设为两级串联运行,第一级滤池水流采用降流式,第二级采用升流式,滤池装填高表面积的陶粒颗粒填料,陶粒粒径2~5mm,填料层厚度1.5~1.8m,垫层采用砾石,厚度0.2~0.3m,滤池滤速控制为0.3~1.0m/h,接触时间1~3h,反冲强度8~12m/h。6. Biological aerated filter process unit: The biological aerated filter is set to operate in two stages in series. The water flow of the first stage filter adopts the downflow type, and the second stage adopts the upflow type. The filter is filled with high surface area ceramsite particles Filler, ceramsite particle size 2-5mm, filler layer thickness 1.5-1.8m, cushion layer made of gravel, thickness 0.2-0.3m, filter filtration rate controlled at 0.3-1.0m/h, contact time 1-3h, recoil Strength 8~12m/h.

本发明的优点在于废水污染物去除效率为高、运行费用低、管理简单,适合于制成一体化设备,安装在中小型天然气采出站现场。该设备对气井采出水中有机物(COD,BOD)、石油类、氨氮、硫化物、悬浮物(SS)等主要污染物均有很好的去除效果。处理后出水能够达到国家《污水综合排放标准GB8978-1996》中二级排放标准。The invention has the advantages of high waste water pollutant removal efficiency, low operation cost and simple management, and is suitable for being made into integrated equipment and installed on the site of small and medium-sized natural gas production stations. The equipment has a good removal effect on organic matter (COD, BOD), petroleum, ammonia nitrogen, sulfide, suspended solids (SS) and other major pollutants in the produced water of gas wells. After treatment, the effluent can reach the second-level discharge standard in the national "Comprehensive Wastewater Discharge Standard GB8978-1996".

附图说明Description of drawings

图1为本发明工艺流程框图。Fig. 1 is a process block diagram of the present invention.

具体实施方式Detailed ways

以处理废水量3m3/d为例,本发明专利的具体实施方式为:Taking the treated wastewater volume of 3m 3 /d as an example, the specific implementation method of the patent of the present invention is as follows:

1、气井采出废水经蓄水池,以0.125m3/h自流进入混凝破乳反应池。反应池搅拌速度100转/min,投加的混凝破乳剂为聚合硫酸铁,破乳剂配比质量百分比浓度为5%。破乳剂的投加量根据废水含CODcr浓度高低,用烧杯试验确定。例如当废水CODcr=5000mg/L时,破乳剂的投加浓度为200mg/L,反应时间控制为5min。1. The waste water produced by the gas well passes through the storage tank and enters the coagulation and demulsification reaction tank by gravity at a rate of 0.125m 3 /h. The stirring speed of the reaction tank is 100 rev/min, the coagulation demulsifier added is polyferric sulfate, and the demulsifier ratio mass percentage concentration is 5%. The dosage of the demulsifier is determined by the beaker test according to the concentration of COD cr in the wastewater. For example, when the wastewater COD cr =5000mg/L, the dosage concentration of the demulsifier is 200mg/L, and the reaction time is controlled at 5min.

2、混凝破乳后的废水,用尼克尼气浮泵抽升,打入竖流气浮池。气浮泵的流量控制为0.125m3/h,吸气量占进水量的7%,气浮池接触区停留5min,分离区停留时间60min;溢流排除浮渣,清水由池底穿孔管引出。2. The waste water after coagulation and demulsification is pumped up with the Niconi air flotation pump and poured into the vertical flow air flotation tank. The flow rate of the air flotation pump is controlled at 0.125m 3 /h, and the suction volume accounts for 7% of the water inflow. The contact zone of the air flotation tank stays for 5 minutes, and the separation zone stays for 60 minutes.

3、在气浮之后废水进入粗滤池。滤池操作滤速为6m/h。3. After air flotation, the waste water enters the coarse filter tank. The filter operation filtration rate is 6m/h.

4、经粗滤池过滤的出水自流流入水解酸化厌氧浮动床生物膜反应器。该反应器投加轻质生物膜颗粒填料,填料投加占池总体积之比为50%(以填料的堆积体积计),操作有机负荷为3kgCODcr/(m3池容·d),水力停留时间7h。4. The effluent filtered by the coarse filter flows into the hydrolytic acidification anaerobic floating bed biofilm reactor by gravity. The reactor is fed with light biofilm particle filler, the ratio of the filler to the total volume of the tank is 50% (based on the bulk volume of the filler), the operating organic load is 3kgCOD cr / (m 3 tank capacity d), hydraulic The residence time is 7h.

5、经水解酸化厌氧浮动床生物膜反应器发生水解酸化的废水,自流进入好氧移动床生物膜反应器。移动床生物膜反应器底部设置穿孔管曝气装置;轻质生物膜颗粒填料投加的体积比为50%,操作有机负荷为1.0kgCODcr/(m3池容·d),水力停留时间7h,曝气量与进水量之比为3∶1。5. The hydrolyzed and acidified anaerobic floating bed biofilm reactor produces waste water that is hydrolyzed and acidified, and enters the aerobic moving bed biofilm reactor by gravity. A perforated tube aeration device is installed at the bottom of the moving bed biofilm reactor; the volume ratio of light biofilm particle filler is 50%, the operating organic load is 1.0kgCOD cr /(m 3 tank capacity d), and the hydraulic retention time is 7h , The ratio of aeration volume to water intake volume is 3:1.

6、好氧移动床生物膜反应器的出水自流进入曝气生物滤池。曝气生物滤池设为两级串联运行,第一级曝气生物滤池水流采用降流式,第二级曝气生物滤池采用升流式。滤池装填的陶粒颗粒填料粒径2~5mm,填料层厚度1.8m,垫层采用砾石,厚度0.3m,滤池滤速控制为1.0m/h,两级滤池的总接触为3h,反冲强度为12m/h。6. The effluent from the aerobic moving bed biofilm reactor flows into the biological aerated filter by gravity. The biological aerated filter is set to operate in two stages in series, the water flow of the first stage of the biological aerated filter adopts the downflow type, and the second stage of the biological aerated filter adopts the upflow type. The particle size of the ceramsite particle filler filled in the filter is 2-5mm, the thickness of the filler layer is 1.8m, the cushion layer is made of gravel, the thickness is 0.3m, the filtration rate of the filter is controlled at 1.0m/h, and the total contact of the two-stage filter is 3h. The recoil strength is 12m/h.

7、由第二级曝气生物滤池的出水自流进入清水池,通过出水泵从清水池将处理好水的抽升排放。出水泵流量为0.125m3/h。不定期用反冲泵从曝气生物滤池抽水,对曝气生物滤池或粗滤池进行反冲。7. The outlet water from the second-stage biological aerated filter flows into the clear water tank by itself, and the treated water is pumped up and discharged from the clear water tank through the outlet pump. The flow rate of the outlet pump is 0.125m 3 /h. From time to time, the backwash pump is used to draw water from the biological aerated filter to backwash the biological aerated filter or the coarse filter.

实施效果:Implementation Effect:

依据以上实施方式,本发明工艺的处理效果为:According to above implementation mode, the treatment effect of technique of the present invention is:

处理水量:3m3/d,水温大于20℃;Treated water volume: 3m 3 /d, water temperature greater than 20°C;

原水主要水质指标:CODcr=2000~30000mg/L,BOD5=1300~7000mg/L,氨氮=29.14~117.3mg/L,石油类=90.3~109mg/L,硫化物=1.84~6.6mg/L,悬浮物(SS)=150~250mg/L。Main water quality indicators of raw water: COD cr =2000~30000mg/L, BOD 5 =1300~7000mg/L, ammonia nitrogen=29.14~117.3mg/L, petroleum=90.3~109mg/L, sulfide=1.84~6.6mg/L , suspended solids (SS) = 150 ~ 250mg/L.

处理后出水满足国家《污水综合排放标准GB9878-1996》规定的二级排放标准。实际出水主要水质指标:CODcr=50~145mg/L(标准为≤150mg/L),BOD5=1.6~12.8mg/L(标准为≤30mg/L),氨氮=0.69~3.95mg/L(标准为≤25mg/L),石油类=0.56~5.47mg/L(标准为≤10mg/L),硫化物=0.0013~0.0342mg/L(标准为≤0.5mg/L),悬浮物(SS)=10.0~30.0mg/L(标准为≤150mg/L)。The treated effluent meets the secondary discharge standard stipulated in the national "Sewage Comprehensive Discharge Standard GB9878-1996". The main water quality indicators of the actual effluent: COD cr =50~145mg/L (standard is ≤150mg/L), BOD 5 =1.6~12.8mg/L (standard is ≤30mg/L), ammonia nitrogen=0.69~3.95mg/L ( Standard is ≤25mg/L), petroleum = 0.56~5.47mg/L (standard is ≤10mg/L), sulfide=0.0013~0.0342mg/L (standard is ≤0.5mg/L), suspended solids (SS) =10.0~30.0mg/L (standard is ≤150mg/L).

Claims (1)

1.一种气井采出废水达标排放的集成化处理工艺,该工艺是对于气井开采过程中排出的含有石油碳氢化合物,硫化物,氨氮及悬浮物的废水达标排放处理,其特征在于包括以下过程:1. An integrated treatment process for the up-to-standard discharge of gas well production waste water, which is for the up-to-standard discharge treatment of waste water containing petroleum hydrocarbons, sulfides, ammonia nitrogen and suspended solids discharged in the gas well exploitation process, and is characterized in that it includes the following process: 1).混凝破乳反应工艺单元:在搅拌速度80-100转/min下,向采出废水加入混凝破乳剂聚合硫酸铁或聚合氯化铝,混凝破乳剂配比质量百分比浓度为5~10%,在气井采出废水含CODcr为2000~50000mg/L的情况下,混凝破乳剂的投加量为50~500mg/L,反应时间控制为3~10min;1). Coagulation and demulsification reaction process unit: at a stirring speed of 80-100 rpm, add coagulation and demulsification agent polyferric sulfate or polyaluminum chloride to the produced wastewater, and the mass percentage concentration of coagulation and demulsification agent is 5-10%, when the COD cr content in gas well production wastewater is 2000-50000mg/L, the dosage of coagulation demulsifier is 50-500mg/L, and the reaction time is controlled at 3-10min; 2).尼克尼气泵气浮分离工艺单元:采用竖流气浮分离工艺,泵的水流量控制为0.1~0.2m3/h,吸气量占进水量的5%~10%,气浮池接触区停留3~5min,分离区停留时间30~60min;溢流排除浮渣,清水由池底穿孔管引出;2).Nickini air pump air flotation separation process unit: vertical flow air flotation separation process is adopted, the water flow rate of the pump is controlled at 0.1~0.2m 3 /h, the suction volume accounts for 5%~10% of the influent water, the contact area of the air flotation tank Stay for 3 to 5 minutes, and stay in the separation zone for 30 to 60 minutes; the overflow removes scum, and the clear water is drawn out from the perforated pipe at the bottom of the pool; 3).粗滤池工艺单元:池内装滤料的粒径级配为5~10mm,2~5mm的颗粒型滤料,滤料层高度为0.7~1.0m,垫层为砾石,高度0.2~0.3m,滤池操作滤速为6~8m/h;3).Coarse filter tank process unit: the particle size distribution of the filter material in the tank is 5-10mm, 2-5mm granular filter material, the height of the filter material layer is 0.7-1.0m, the cushion layer is gravel, the height is 0.2- 0.3m, the operating filter rate of the filter is 6-8m/h; 4).水解酸化厌氧浮动床生物膜反应器工艺单元:反应器投加轻质生物膜颗粒填料,以填料的堆积体积计,填料投加量占池总体积之比为50%~70%,当进入生物膜反应器废水的CODcr为400~2000mg/L时,操作有机负荷为1~5kgCODcr/(m3池容·d),水力停留时间5~8h;4). Process unit of hydrolytic acidification anaerobic floating bed biofilm reactor: light biofilm particle filler is added to the reactor, and based on the bulk volume of the filler, the ratio of the amount of filler to the total volume of the tank is 50% to 70% , when the COD cr of the wastewater entering the biofilm reactor is 400-2000mg/L, the operating organic load is 1-5kgCOD cr /(m 3 pool capacity d), and the hydraulic retention time is 5-8h; 5).好氧移动床生物膜反应器工艺单元:移动床生物膜反应器中也投加轻质生物膜颗粒填料,并在该反应器底部设置曝气装置,以填料的堆积体积计,填料投加量占池总体积之比为50%~70%,操作有机负荷为0.5~2kgCODcr/(m3池容·d),水力停留时间5~8h,曝气量与进水量之比为3~10∶1;5).Aerobic moving bed biofilm reactor process unit: light biofilm particle filler is also added to the moving bed biofilm reactor, and an aeration device is installed at the bottom of the reactor. Based on the bulk volume of the filler, the filler The ratio of dosage to the total volume of the tank is 50% to 70%, the operating organic load is 0.5 to 2kgCOD cr /(m 3 tank capacity d), the hydraulic retention time is 5 to 8h, and the ratio of aeration to water inflow is 3~10:1; 6).曝气生物滤池工艺单元:曝气生物滤池设为两级串联运行,第一级滤池水流采用降流式,第二级采用升流式,滤池装填高表面积的陶粒颗粒填料,陶粒粒径2~5mm,填料层厚度1.5~1.8m,垫层采用砾石,厚度0.2~0.3m,滤池滤速控制为0.3~1.0m/h,接触时间1~3h,反冲强度8~12m/h。6). Biological aerated filter process unit: The biological aerated filter is set to operate in two stages in series. The water flow of the first stage filter adopts the downflow type, and the second stage adopts the upflow type. The filter tank is filled with high surface area ceramsite Granular filler, ceramsite particle size 2-5mm, filler layer thickness 1.5-1.8m, cushion layer made of gravel, thickness 0.2-0.3m, filter filtration rate controlled at 0.3-1.0m/h, contact time 1-3h, reverse The impact strength is 8~12m/h.
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